Power Generation

Sicomp Control System Upgrade.

Upgrade of ageing 1985 control system with 3000+ I/O points through targeted replacement and SCADA integration.

The Challenge

Legacy System Failures

The original 1985 Sicomp control system was becoming increasingly unreliable, threatening plant continuity.

Cost of Full Replacement

A complete system overhaul was impractical due to the scale—over 3,000 I/O points made full replacement cost-prohibitive.

Integration Complexity

Maintaining continuity while upgrading required precise mapping between legacy hardware and modern interfaces.

The Solution

Analysed failure patterns to target only critical components for replacement.

Designed a new interface card to bridge legacy I/O with modern control systems.

Implemented a new SCADA and HMI for improved control and visualisation.

Completed the upgrade without triggering system downtime.

What We Offer

Targeted Legacy System Upgrades

Cost-efficient solutions for high-I/O ageing systems.

Custom Interface Design

Bridging legacy hardware with new-generation controls.

SCADA & HMI Modernisation

Delivered intuitive visual control and diagnostics.

Zero-Downtime Implementation

All changes made while maintaining live operations.

Project Scope

System Audit

Identified points of failure within the existing Sicomp infrastructure.

Hardware Integration

Developed interface cards to connect legacy I/O to new controls.

Software Modernisation

Installed and configured updated SCADA and HMI platforms.

Commissioning & Handover

Delivered complete upgrade with no safety or production incidents.

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Our Safety Commitment

All upgrades were performed without any safety incidents or operational disruptions. The approach protected existing infrastructure while delivering modern functionality with zero downtime.

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